Second Interim Statement IN-005/2014

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Transcription:

Second Interim Statement IN-005/2014 Serious incident occurred on 9 March 2014 at Tenerife South / Reina Sofía airport (Santa Cruz de Tenerife, Spain) to aircraft Boeing MD-11, registration PH-MCU GOBIERNO DE ESPAÑA MINISTERIO DE FOMENTO

Second Interim Statement IN-005/2014 Serious incident occurred on 9 March 2014 at Tenerife South / Reina Sofía airport (Santa Cruz de Tenerife, Spain) to aircraft Boeing MD-11, registration PH-MCU SUBSECRETARÍA GOBIERNO DE ESPAÑA MINISTERIO DE FOMENTO COMISIÓN DE INVESTIGACIÓN DE ACCIDENTES E INCIDENTES DE AVIACIÓN CIVIL

Edita: Centro de Publicaciones Secretaría General Técnica Ministerio de Fomento NIPO: 161-16-192-3 COMISIÓN DE INVESTIGACIÓN DE ACCIDENTES E INCIDENTES DE AVIACIÓN CIVIL Tel.: +34 91 597 89 63 E-mail: ciaiac@fomento.es C/ Fruela, 6 Fax: +34 91 463 55 35 http//www.ciaiac.es 28011 Madrid (España)

Important notice This document constitutes the interim statement envisioned in Article 16.7 of Regulation (EU) no. 996/2010 of the European Parliament and of the Council, as well as in paragraph 6.6 of Annex 13 to the Convention on International Civil Aviation. The statement includes the details of the progress of the investigation and the most important operational safety issues revealed to date. The information provided herein is subject to change as the investigation proceeds. Pursuant to the contents of Regulation (EU) no. 96/2010 of the European Parliament and of the Council and of Annex 13 to the Convention on International Civil Aviation, the investigation is purely technical in nature and is not intended to determine or apportion blame or liability. The investigation is being conducted without necessarily resorting to evidentiary procedures and for the sole purpose of preventing future accidents. Consequently, the use of this information for any purpose other than to prevent future accidents may result in faulty conclusions or interpretations.

Second Interim Statement IN-005/2014 Abbreviations ºC Degrees centigrades ATC ATPL(A) FL h HPT LPT n.º N2 Air Traffic Control Airline Transport Pilot License (Aircraft) Flight Level Hour (s) High Pressure Turbine Low Pressure Turbine Number Rotation speed of the HP turbine/compressor assembly iv

Second Interim Statement IN-005/2014 DATA SUMMARY LOCATION Date and time Sunday, 9 March 2014; 00:30 local time 1 Site AIRCRAFT Registration Type and model Operator ENGINES Type and model Tenerife South/Reina Sofía airport (Santa Cruz de Tenerife, Spain) PH-MCU Boeing MD-11 Martinair Cargo Pratt & Whitney PW4000 Number 3 CREW Captain First Officer Age 47 years 40 years old License ATPL (A) ATPL (A) Total flight hours 15520 h 11620 h Flight hours on the type 8304 h 3880 h INJURIES Fatal Serious Minor / None Crew 2 Passengers 1 Third persons DAMAGE Aircraft Third parties Minor None FLIGHT DATA Opeation Phase of flight Commercial Air Transport - Scheduled - International - Cargo Take-off REPORT Date of approval 24 February 2016 1 At the date of the accident the local time is the same as UTC. v

Second Interim Statement IN-005/2014 1. SUMMARY OF THE FLIGHT Aircraft Boeing MD-11, registration PH-MCU, was scheduled from Amsterdam (The Netherlands) to Viracopos (Brazil), with a step-over at Tenerife South/Reina Sofía airport (Spain) During the take-off at Tenerife South, when the aircraft was at initial climb, the crew heard an anomalous noise and noticed that the aircraft yawed to the right. Shortly afterwards they felt vibrations and observed the engine indications, seeing that the parameters corresponding to engine n.º 3 were not normal. N2 was at 105% and the exhaust temperature was about 875ºC. They concluded that engine n.º 3 had suffered severe damage. They started to apply the pertinent procedure, and while doing it, they observed that the engine n.º 3 fire alarm activated. The crew kept applying the procedure they were performing (applied when there is severe damage or engine fire). The fire alarm went off after discharging the first fire extinguishing bottle. They decided to return to departure airport. They assessed the situation, and considering that the fire alarm had gone off and that they were in good condition to control the aircraft, they decided to discharge fuel in order to diminish weight at landing, before returning the Tenerife South airport. They asked authorization to ATC to discharge fuel at FL070, being cleared to do so. They climbed to FL070, and once the necessary fuel load was discharged, they proceeded to return to Tenerife South airport, where they landed without further notice. Once in the platform a visual inspection was made, realizing that the engine n.º 3 had suffered an uncontained break, originated by a blade breakage. No fuel, hydraulic liquid or oil leaks were observed. As a consequence of the breakage and the subsequent material output from the engine some damage was produced affecting: Pylon and engine n.º 3 nacelle. Right wing Horizontal stalibizer 1

Second Interim Statement IN-005/2014 2. STATUS OF THE INVESTIGATION The investigation has focused in establishing the damage suffered in engine n.º 3, trying to identify their sequence. On that purpose the engine was detached and sent to the maintenance shop in Singapore, where the last overhaul was performed. There the engine was disassembled and inspected. All the damage of the engine, mainly affecting the four stages of the Low Pressure Turbine (LPT) have been identified and documented, and first hypotheses of the failure sequence have been established. The second stages of the High Pressure Turbine (HPT) as well as all stages of LPT were sent to manufacturer facilities to further inspect them and perform the necessary metallographic analyses. Measurements were made on the second stage disk of the LPT, as well as metallographic analysis of airfoils and vanes of the fourth stage of the LPT, in order to determine what the sequence of the fractures was, as well as its root cause. 3. NEXT STEPS The investigation has been finished and the final report will be published shortly. 2